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Tim Nielsen - Meeting Report
We arrived at the track pretty early on Friday afternoon as we
had a few thing to do before we hit the track. Firstly we had to
get scrutineered as we were on the audit list. Once all the
paperwork was completed we were back in the pits adjusting the
new fuel system. With the dragster warmed up, we were ready to
hit the track. There was only around 80 cars for this event, so
we were hoping that we could get a handful of runs in.
Our first pass was at 5:54pm. Everything felt and seemed ok
until we got the timecard back. Our 60ft time was off big time,
the track felt sticky under foot, but the 60 was just not there.
We adjusted the fuel system and changed jets then headed out for
our second pass at 7:00pm. Our 60ft was the same while the EGT
readings were really high for this run. Back in the pits we
pulled the plugs out of the engine they all looked fine. We
adjusted the float levels on the carby then headed out for our
third pass at 7:44pm. |
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Our EGT got back to were they should
be, but the 60ft stayed the same as the previous two pass. We
finally came to the conclusion that the start line conditions
were not that favourable on the night. We made a few more
adjustments back in the pits then headed out for another pass.
Our 60ft improved and finally we were heading in the right
direction. I had a good run against Paul Partridge in his Big
Block powered Mustang, a good side by side pass up until the
1000ft mark until the Big Block powered took over.
With that being run number 497 on my engine, we decided that if
we could finish on 499 runs for the evening we would be happy.
It was 9:39pm and we backed up the previous pass with the time
slip being almost identical. Back in the pits we made one more
adjustment to the fuel system, then headed back out for our last
pass for the evening. When we arrived at the start of the
staging lanes the barriers were up and the lanes were closed for
the night. We went down anyway and they allowed us through for
one last pass. It was 10:30pm and run number 499. We proceeded
with a long burnout and everything improved on the run and this
being the quickest pass of the night.
Next meeting will be run number 500 on my Aluminium Rodded Small
Block Chev. |
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