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Tim Nielsen - Meeting Report
The day had arrived and the small block chev was about to its
500 pass down the dragstrip. With all the hype leading up to
this pass, the burnout was a big let down. The engine seemed to
bog as I hit the throttle then cleared, but it was crap. The
engine got up on the 2 step as usual but everything was wrong,
the dragster stepped out at around 300ft but I kept into it as
it didn't feel that bad; and it was the engines 500 pass. The
time card was not even worth looking at and the EGT showed that
we were still a little rich. |
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Back in the pits we re-jetted the carby
and headed out for pass # 501. The burnout was weird, while I
was half way through the burnout the engine seemed to pull down,
then it revved up again and continued on.
Once in stage I jumped on the throttle and the engine almost
stalled, I still had the throttle at Wide Open Throttle and the
revs picked up again. It left the line like a an old mole, with
the 60ft being 1.65 |
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Once the dragster got going a little it
picked up and I ran the full 1/4 mile.
When I got to the turn off at the end of the track I bumped the
engine back into 2nd gear to get around the corner and the
converter made some ugly sounds. I put it into neutral and the
noise went away, I put it back into 2nd and the noise came back,
time to shut the engine down, the converter is now rooted. |
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Copyright © Shiredragracing - All
rights reserved - 2011
www.1320webdesign.com.au -
Tim Nielsen 0425 265 763
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